Fall is over here in Winnipeg, and my project car work is winding down for the year due to my unheated, un-insulated working space. I just bought a new house to move home and ended up with something I really liked, but the garage leaves a lot to be desired. I effectively moved in at the beginning of September, and re-started working on the Neon half way through October. Fresh out of the barn after 8 years, it weathered well in some ways, and poorly in others.
The ancient RT-615s can finally retire. A set of Neon bubbles with 2005 date coded RA1s will take over.
Rodents really went to town and ruined most of the interior in the past year, and a lot of the bolt-on stuff to the chassis rusted. If I hadn't bought a boatload of parts for it this past year, I probably would've (and should've) given up on it. But the chassis is still good and there are lots of bright spots to this car, so on we go.
The interior after being gutted and scrubbed of the rodents. I fixed up a few wires that had been chewed through, but I still need a new carpet and new seats. The headliner is being recovered with new fabric soon, and I'll pull the rest of the dash out to clean out the HVAC in the spring. The car smells okay now, so that problem is solved.
The car suffers from most of the routine Neon issues and most fixes are well-known, like 3D-printed window regulators, and a lot of DIYing to fix the annoying issues.
Anyway, the car drove into my garage from the tow truck, on 8+ year old gas, and crossed the finish line right when the fuel line blew out at the tank. Pretty impressive that a janky car on 8+ year old fuel could actually do it. A compression test showed bad results though, 215 - 200 - 120 - 200. The car had overheating issues that the previous owner failed to fix correctly, which likely lead to a combustion sealing failure. The fan control module usually fails on Neons, but instead of replacing it - the previous owner tried to replace ECUs, and eventually hardwired the fan - anything but properly diagnose the problem. I pulled the cooling system apart, and it was pure milkshake with rotten water pipes, a leaky radiator, a failed thermostat, and likely a warped head. It's ALL getting changed.
The block is really ugly, possibly the worst I've seen cosmetically. It also leaks oil out of every orifice - the rear main coated everything.
Despite the highish mileage (260,000 km or 161,500 miles), and long history of neglect, the head looked good. It ran nice with no funny noises, as I recall. I bought an entire exhaust system (TTi mid-tube header, NOS Mopar catalytic converter, TruBendz 2.25" piping and Borla muffler), when it turns out that the exhaust is in great condition other than a cracked manifold and rotten muffler. Oops.
Big thanks to GRMer Run Away for coming by to unjam the CVs from the transmission for me.
Anyway, this car has always had a really strange clutch pedal, which is why the engine/trans came out in the first place. Its engagement point varied so much, I figured all the clutch cables that came with the car all had the same failure that prevented them from keeping the clutch motion consistent. When we pulled off the transmission, we found out why. It became obvious that someone had been in there when some of the transmission bolts were loose, some were missing (!!), and for whatever reason, previous owner installed a Valeo non-modular clutch in this car. They went through the trouble of finding a rareish flywheel, lined it up, slapped it together and called it a day instead of buying a modular clutch kit. That's fine by itself, but the problem is that they didn't replace the pivot ball, which failed, and things went south from there. The clutch has very little use, but the pressure plate is ruined from bad alignment. Fingers are missing, the ones that remain are jagged blades, because the TOB wore through them and was likely on its way to total clutch failure very shortly. So once again, the previous owner did a poor fix on the car and then couldn't figure out why the car continued to misbehave, so they just kicked the can down the road. My $42 RockAuto LuK PT Cruiser clutch, NOS Mopar clutch cable, Mopar clutch pivot ball, TOB, and a donated flexplate will put this all together the way it was meant to be. I won't tolerate any more clutch issues!
But wait, there's more! Not only did this gorilla totally botch the clutch job by cheaping out, they also wrecked several of the flywheel bolt threads on the crankshaft! These crankshafts are extremely hard to find here, there are simply no Neon 2.0L engines around. Shipping one to me is atrociously expensive, so that's out. My dad is optimistic that the machine shop he's dealt with for decades will fix this at a reasonable price, and I'm hopeful. The bills are really piling up on this car. The block needs a tanking and a decking at least, plus the crank fix, in addition to a head decking (which will be used as an excuse to crank up the compression). With that, a junkyard 2.4L is looking really appealing to save money.
Neons are not very well prepared for the elements and they typically died quick deaths in Canada. This one is the highest mileage Neon I've had, so it should've fared the worst. Despite that, I never really realized that the chassis and surrounding stuff is still really good, and there is nothing that a bit of grinding and touch-up can't handle quickly. I'm stoked that the body still looks this good after 25 years! I'll clean up whatever surface rust I can this winter & spring; with most of the bolt-on stuff being replaced, it should look good regardless. The rockers are a known rust spot on Neons, but both look great inside and have already been covered in Fluid Film to keep them from ever rotting out.
After struggling for a bit tearing the engine down last night, I came back today with an air impact and they came off easy. And the news is.....good?!
Somehow the bores still look nearly new. Great cross-hatch, no ridge, very little up/down wear evident. I'm confident these bores are still good, so they'll get a dingleball hone and maybe some new EngineTech moly rings ($27 USD!), and should be good as new. If the pistons show abnormal wear, I'd be happy with a set of standard bore EngineTechs ($68.29 USD!!!) and everything would be fresh. The cylinder head looks really good, no damage evident anywhere. I'll assume it's still warped, which I think is a safe assumption. A friend of mine offered up a DOHC head that's ported on the intake side for free; I'm thinking about bringing that cylinder head, plus my ported 420A head to a machine shop and asking them to replicate the exhaust port work. Or, we could throw the BC valve train from the 420A head into this one and run on stock ports. Undecided, but there are some choices here. I'm trying to get a set of Crane 16s or Crower S2s to use instead of modifying the BC 420A cams.
Situation as of last night, not much is likely to change before the snow melts. Once the engine is refurbished and the trans comes back from the cleaning & LSD/input bearing install, it should go together very quickly.