Apr 2, 2009 update on VWguyBruce's 1986 Volkswagen Jetta GLi

3 Cylinder Operation Corrected

Whilst running the autox the other day the car was only revving to 4000rpm and #4 cylinder wasn’t firing at all. Well, I am happy to say I corrected the problem and the car is running like a champ. It turns out that the guy who was cleaning the intake boot incorrectly installed the screen upside down. As a result the FI plunger was not coming up for hitting the upside down screen and the fuel distributor wasn’t pumping any fuel to #4 and very little to the other cylinders. Screen is now gone for good. So, it turns out I’m a dork and learned a lot about CIS-E in the process.

On the plus side, the compression in #4 was over 170psi and held very well. I’m pleased since the odometer reads over 200k miles. Who knows if it’s the original motor but at least it’s running right now.

 

Our Preferred Partners
wcTWTvHQv701SQt2fzV2wxJbctZdWKT3HBrAYlPui4yQNPxvKm40UDnVu7LOBBlO