So, back from the Challenge and (moderately) rested.
On the whole, I would call the trip to the Challenge this year a success. I ended up taking 26th-place in a field of 40 cars that made the final results (I believe a total of 46 entered, but not all made it), putting the (or at least 'my') Rampage in the bottom of the top 2/3s of the entries. Both its autocross and drag times were solidly in the middle of the pack, running a 41.42 in the cones and a 17.408 down the strip, and I took the 'Don't Judge Me' option on the concourse, knowing that in the shape it's in now the car would most likely far poorly in the concourse.
The weekend was not without its issues... honestly, at 10pm on the night we were supposed to load it up onto the trailer to leave the next morning, I was still seriously debating whether or not to take the car at all. Ultimately despite its still having issues, we were hopeful that we had resolved the major one I had been concerned with and figured that at minimum the car could make at least a successful autocross run and a drag run, so we may as well try.
Before leaving though, there was one kink in the works (that also contributed to not being sure it was worth going) which was that singleslammer- who was going to the Challenge and bringing the race tires I planned to use- got in touch with me and let me know that they had broken down and had to turn around and thus would not be making the event. So leaving for Florida, I didn't know if I was going to have a set of tires to run on (having already pulled the older street tires off the wheels I'd planned to use).
Once we got down to the hotel, we pulled the car off the trailer to test it out- we had just figured out before loading it both why the turbo didn't seem to be spooling and why I wasn't seeing any boost on the boost gauge (believe it or not, these were different issues...). However in testing it out on the road, the car just felt really sluggish. After a lot of futzing with things and finally working out how to hook up the check engine light, we managed to read the codes and find that there was an issue with the #1 injector bank- and on closer inspection found that the #2 cylinder injector plug wasn't firmly seated and the car had been running on 3 cylinders. That resolved, it ran solidly better.
When we got to the track the next day, I met up with Stampie and coordinated to get a set of 13" diameter NINE INCH WIDE 4x100 wheels & sticky tires to run. After checking out that they would not rub on the body work (too much), it was off to the autocross runs. My first two runs were pretty bad, given I've driven around an autocross course only a handful of times- all of which have been at the Challenge. The pro did a much better job, turning in a 41.420 run- which ended up being only 1/4 of a second slower than my non-teammate teammates' Miata (and faster than another Miata). The car didn't have any significant problems beyond those I couldn't really do much about- like having the struts and shocks that came with it on it still and having done barely any aligning.
The drags later that night however were a bit different of a story. The first run I ran like an 18.2, and it was clear that the car was NOT performing anywhere near its best. For starters, the tires that had worked great on the autocross felt like I slipped for a LONG time on the launch at the drag, and it seemed like (and I confirmed) I wasn't getting boost toward the end. The tires I couldn't really do much about, but the boost I had a pretty good idea of what was wrong and quickly confirmed this: the wastegate actuator lever had fallen off the wastegate itself so the car wasn't building any boost. While (with lots of protective clothing) able to get the actuator hooked up agian, we could NOT get a pin in to keep it from coming off again (I really hate FCA's engineers for this one- it's COMPLETELY backwards from what would seem logical and nigh impossible to do anything about when the engine is on the car and put together).
After a LONG time of fighting with it, I decided we weren't going to be able to get the pin into place and took the car out for one more run with the hopes that it wouldn't come off again. This time I didn't try and launch so hard, and could tell that I didn't lose the turbo until after the 2/3 shift (I think I lost it at 1/2 the first run), and while I don't think the tires slipped as much the car was a NIGHTMARE to try and keep straight, as near as we can figure from the width of the tires and torque steer. This led to my putting down a 17.408 run time- an improvement, but not near what the car/engine combo should have been capable of.
The major upshot of the weekend was making the decision (pretty early on) that I WILL be bringing this car back next year after having a full year to get things sorted and figured out. I know that it's capable of a lot more than it did this year (certainly in the drags and concourse, and likely on the autox as well), and I want the chance to get it there and to improve on it. Plus, it's just a really fun little car that I will be happy to hold on to and improve.
Many, many thanks to eastsidemav (and his wife), Jerry, and wae for their help over the weekend working on and transporting the car; to Vigo for all his advice both before and at the event (and over the next year ) about turbo Dodges; to Stampie for helping with the tires & wheels, and the many other GRMers who lent advice, tools, and encouragement over the course of the event.
Here's a few photos of the car from the weekend:
https://www.flickr.com/photos/wesleyhetrick/37809342942/in/album-72157688178100634/